High Deviation Hybrid Plug

A major North Sea operator was evaluating the options available for setting a deep-set plug in a well with a target depth of approximately 11,000ft and a deviation of 80. The completion included a landing nipple situated below the production packer. This presented the opportunity to use a conventional lock mandrel style plug.

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